翻訳と辞書
Words near each other
・ Fußball ist unser Leben
・ Fußballtrainer Wulff
・ Fußgönheim
・ Fučkovci
・ Fučík
・ Fułki
・ Fužina, Ivančna Gorica
・ Fužine
・ Fužine Bridge
・ Fužine, Croatia
・ Fužine, Gorenja Vas–Poljane
・ Fužinski bluz
・ FV
・ FV 09 Weinheim
・ FV 1897 Linden
FV Alaska Ranger
・ FV Athena
・ FV August Wriedt
・ FV Bad Vilbel
・ FV Biberach
・ FV Biebrich
・ FV Big Valley
・ FV Cornelia Marie
・ FV Diefflen
・ FV Dresden 06
・ FV Ekawat Nava 5
・ FV Empire Fisher
・ FV Engers 07
・ FV Gaul
・ FV Illertissen


Dictionary Lists
翻訳と辞書 辞書検索 [ 開発暫定版 ]
スポンサード リンク

FV Alaska Ranger : ウィキペディア英語版
FV Alaska Ranger

FV ''Alaska Ranger'' was a fishing factory ship owned and operated by the Fishing Company of Alaska of Seattle, Washington. The ship was constructed in 1973 for use as an oil field service vessel. The ship sank 23 March 2008, after reporting progressive flooding only hours earlier. Of the 47 on board, 42 were rescued. Of the five fatalities, four were recovered dead, and one was never found. The Coast Guard was initially misinformed about the number of persons on board the vessel, and secured the search with one crew member still unaccounted for. After realizing there was still one person missing, the Coast Guard reinstated the search, but did not find the crew member.
==Sinking==

According to the United States NTSB (National Transportation Safety Board), the triggering event in the sinking was the loss of one of the two rudders. This allowed water to pour into the rudder room by way of the 9-inch diameter rudder trunk. The marine architect designed the opening of the rudder trunks to be above the waterline so that water would not enter the rudder room should a rudder fall out. However, United Marine Shipbuilding changed the ship from an oil well service boat to a fishing boat in 1988. The changes raised the waterline 2.5 feet. This put the rudder trunk openings below the water line. The ceiling of the rudder room was only 20 inches above the trunk openings. Flooding of the rudder room should not have sunk the ship since there was a watertight bulkhead. The NTSB can only speculate that the door was left open, the seals or latching dogs failed, or that the holes cut in the bulkhead for refrigeration lines needed for fish processing were not watertight. If the conversion installed a watertight bulkhead between sections of the fish processing area the boat would not have sunk. Whatever the reason, the water flooded the engine room. At some point the water level became high enough to short out the main electrical distribution panel. This caused the loss of electrical power throughout the boat.
The boat had variable-pitch propellers. This means the captain can keep the diesel engines at a constant RPM needed for the ac electrical generators, and use the variable pitch to change boat speed or reverse direction. The variable-pitch propellers used a hydraulic actuation system. As designed, there was one electrical hydraulic pump and one engine-driven mechanical hydraulic pump for each propeller. In 1989, Transmarine Propulsion Systems replaced both mechanical pumps with electric pumps, saying they could not get parts for the mechanical pumps.
With electrical power lost, all 4 hydraulic pumps stopped. With no hydraulic pressure, hydrodynamic forces on the propellers caused the pitch to reverse. This made the boat run full astern. The rearward motion of the boat drove the sinking aft section further under water. It also exacerbated water entry into the air intake vents on the trawl deck.
The captain of ''Alaska Ranger'' died in the sinking so it is unknown why he did not stop the diesel engines. The Coast Guard had tested the engine emergency shutoff system a year before the sinking and reported that it functioned properly. The boat moving full astern meant that two of the three lifeboats were separated from the ship. This meant that 25 crew members that had jumped into the water never got to one of the three lifeboats.
United States Coast Guard Marine Board of Investigation
The United States Coast Guard also investigated the sinking through a Marine Board of Investigation. The Marine Board's Report of Investigation determined a different scenario related to the cause of the casualty. The Marine Board reviewed thousands of pages of documents and photographs related to the maintenance and repair of the vessel, and examined in-depth the installation of the Kort nozzles. The Marine Board also examined in detail the rudder installation.
As a result of this analysis the report concludes that "Though the exact initiating event that created the source of flooding is unknown, it was likely related to the poor material condition of the vessel and may have been related to the Kort nozzle struts which are believed to have experienced excessive stresses where they were attached to the hull."

抄文引用元・出典: フリー百科事典『 ウィキペディア(Wikipedia)
ウィキペディアで「FV Alaska Ranger」の詳細全文を読む



スポンサード リンク
翻訳と辞書 : 翻訳のためのインターネットリソース

Copyright(C) kotoba.ne.jp 1997-2016. All Rights Reserved.